Free-Free Impact Modal Test of Shaft & Roll ResultsModal Analysis test results of Feed Roll & Shaft... Typically this would not be considered a good test setup, however; the test shoul
Trang 1Free-Free Impact Modal Test of Shaft & Roll Results
Modal Analysis test results of Feed Roll & Shaft Most bending is indicated in the shaft as
X
Y Z
1 2 3 4 5 6 7
1 2
Trang 2Figure 2: Rotor model, third mode 10,862 CPM Bending occurring in the shaft but not
in the roll, which is primarily a very stiff hollow cylinder The bolted joint was modeled as solid.
Figure 3: Frequency response function (FRF) of the Driving Point, Bottom Plot
Coherence of the measurement is shown in the top plot The data becomes noisy
above 500Hz because the instrumented hammer tip was not hard enough to input
adequate energy into the rotor to excite the structure in this frequency region
The FRF of the Driving Point shows
frequency of the shaft-roll at 187 Hz ~ 11,220 cpm
The rotor model calculated to 181 Hz
~ 10,860 cpm or 96.8%
Trang 3Shaft & Roll Installed Impact Modal Test.
as indicated by the red dots.
Note that the response will be affected by any
looseness in the bearing assembles This may
cause non-linearity in the response and
reduce coherence Typically this would not be
considered a good test setup, however; the
test should be useful in identifying potential
problems such as loose bolts, traverse shaft
crack, and looseness in the bearing assembly
Step Two
Trang 4Installed Shaft & Roll Impact Modal Test.
the bearings.
the roll.
Trang 5Installed Shaft & Roll Impact Modal Test.
the bearings.
the roll.
Trang 6The rotor model predicted the shaft-roll first flexure mode with the shaft
supported by bearings (Brg Stiffness Estimated) at 10,208 cpm ~ 170 Hz.
Trang 7The measured FRF showed a fairly narrow range of resonance for
the 1st flexure mode In the FRF plotted, the resonance measured
204.38 Hz ~ 12,263 CPM
!
Trang 8Draw Roll-Shaft Natural Freq in Hz.
Results from one machine with 23 shaft-rolls All of the rotors “rang”
except the #2 Disassembly of the #2 roll showed loose bolts The rolls
natural frequency were in the 200 Hz range with exception of roll 21.
Trang 9Roll Response Measured By Im pact Modal Test
Trang 10Shaft-Rolls Lbf/Mil (Dynam ic Stiffness)
Trang 11The FRF from Roll #2 did not show a natural frequency Typically, modal analysis requires a linear structure but in this case we are looking for a non- linear structure with poor resonance qualities
Inspection showed a loose bolted joint
Trang 12Step Three
Bump Test of Installed Shaft-Roll Assembly To Identify Defective Rotors
Compare impact data from triggered spectrum & time waveform to modal data (FRF) tests for location of roll natural frequencies
Monitor natural frequencies during operation for shifting
(A shift lower would indicate a change in the stiffness of some components in the system such as broken bolts, shaft traverse crack, bearing assembly looseness.) Follow-up with modal testing on as
needed basis
Trang 13Step Three
Bump Test of Installed Shaft-Roll Assembly To Identify Defective Rotors
Bump testing did not prove to be useful in detecting shafts with loose
or broken bolts
After several tests, it was discontinued.
Trang 15+
Trang 16Example of time waveform and spectrum from a roll The FFT shows 12.46 mils P-P run out The time waveform shows much less amplitude P-P due
to roll off of the accelerometer The FFT is multiplied by a curve to
compensate for the roll off and yields the correct amplitude
Trang 17This roll measured 37.6 mils runout Note the time waveform clearly shows asymmetrical stiffness indicating a loose joint
Trang 18Frame Roll ID WO # Status Last Read Bearings Last Read Radial Runout Last Read Stiffness Worked
11/16/01 Update: Feedroll and Drawroll Condition
Spreadsheets with color coding were used for reporting the
condition of Roll-Shaft Bearings and Bolted Joint indicated condition.
Roll run out tolerance measured at the end of the roll:
> 30 Mils Schedule Maintenance
for inspection of bolts
10 Mil to 30 Mil Monitor More
Frequently
Trang 191 Modal testing was successful in identifying shaft-roll rotors with lower
stiffness, i.e., did not ring when impacted as likely candidate of loose
bolting, failed bolting, or shaft with a developing crack.
Detection Process:
2 The roll rider data was useful in identifying rolls with loose bolting
Limits were established as follows:
1 <10 Mill acceptable
2 > 15
3 > 30 Mill PP Schedule inspection of the bolts.
3 Vibration data
A Collected using the long stinger in the end of the roll cover plate
was successful in detecting defective bearings.
4 Physical inspection of bolting, shaft and roll mating faces, condition of
tapped holes, bearing fits, etc
B Data from permanent accelerometers installed on the bearing
housings were not as useful in detecting bearing defects as data collected on the end of the rolls.
Trang 201 The roll and shaft mating surface finish, flatness, hole angularity and
depth of full thread tolerances were enforced by inspection at the
repair shops
Correction Process:
2 The bolt length was reduced ½” to 6”.
3 Thread lubricant was changed to Loc-Tite Graphite which has a very
low K factor.
4 Bearing heating procedures were modified to use a temperature
controlled heater for all bearing installations.
Trang 211 Use of Modal testing to detect loose rolls was effective But, testing had
to be scheduled when a line was down We were not aware that this test method had been used previously.
2 The roll rider block with accelerometer is a modification of a well know
test method using a wood stick also called a beaver tail (sold by IRD)
After some modification of the initial block design and data collection methods, the test proved successful in identifying rolls with excessive run out
3 Vendor shop visits were very helpful to improve understanding of
the repair processes and identify problem areas
4 Modification of the repair processes, tightening of tolerances, initiation
of inspections of repaired Shafts & Rolls with documentation were
successful in improving the quality of Shaft & Roll repairs performed by repair shops.
Trang 225 Modification of Bearing and Roll maintenance installation practices
proved successful in reducing the number of improperly installed shaft assemblies.
Trang 23roll-Roll Shafts With Bolt Failures
were not identified.
No data available before
1997
Trang 24Bearing Failures in 2003 reduced 79% compared to 2002
Lowest number of failures documented over 10 years.