in the final motor setup, a part of metal has four webs of 15 mm thickness and each is added by welding to the lower motor Motor upper bearing Motor lower bearing Figure 2 Vibration spect
Trang 1ORIGINAL ARTICLE
Finite element analysis for structural modification
and control resonance of a vertical pump
Dalia M El-Gazzar
Mechanical & Electrical Research Institute, National Water Research Centre, Ministry of Water Resources & Irrigation,
Delta Barrage, Egypt
Received 23 October 2016; revised 22 January 2017; accepted 13 February 2017
KEYWORDS
Vibration;
Vertical pump;
Modal analysis
Abstract The main objective of this research was to evaluate and enhance dynamic performance for a vertical pumping unit The original electric motor of the pump unit had been replaced by another one different in design and weights Vibration has been increased greatly after installing the new motor Consequently, it is necessary to estimate the change in the vibration characteristics owing to the difference in the boundary conditions of the new motor Measured vibration levels and frequency analysis were dangerous at 1 due to resonance problem Finite Element Analysis was used to model the motor structure in order to find its natural frequencies and mode shapes The results confirm that the third natural frequency is very close to 1 operating speed with deviation about 1% To solve the resonance problem, it was recommended to increase the structure stiffness The results after modifications confirmed that the overall vibration level decreases by 89%
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1 Introduction
The pumping system is the most important water system
sup-plying water for irrigation and removing subsurface water for
drainage purposes There are more than 2000 large scale
irriga-tion and drainage pumping stairriga-tions in Egypt operating under
different conditions Pumping stations in Egypt are subjected
to many problems
Podugu[1]indicated that the sources of vibration in pumps
can be categorized into three types such as mechanical,
hydraulic and peripheral causes Imbalance and misalignment are the major reasons for mechanical problems Peripheral causes of vibration include harmonic vibration from nearby equipment or drivers, operating the pump at critical speed Problems with any of these issues will show up as symptoms, showing higher than normal vibration at certain key frequencies
Redmond and Hussain[2]analyzed the vibration resulting from a simple linear rotor model on isotropic supports and showed the dominant response to be similar to that resulting from a shaft bow The predicted vibration response did not contain any second-harmonic content The reliability and per-formance of any pump system can be directly affected by its dynamic characteristics Sinha and Rao[3]conducted Modal E-mail address: dalia_engdalia@yahoo.com
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Trang 2analysis on the complete assembly of pumps and piping layout
and identified resonance as the root cause for pump failure
DeMatteo [4] stated that modal techniques are powerful
tools that enhance an analyst’s ability to understand the
sources of vibration A case history of the vertical pump was
investigated Testing progression from problem identification
in route vibration measurements to resonance testing was
pre-sented Resonance problems are difficult to solve Modal
Anal-ysis gives a clear picture of the machine’s motion; however,
neither tool has the capability to solve resonance problems
Marenco[5], has experimentally investigated the effect of
bearing housing design will influence the dynamic
characteris-tics of the system In this paper, an attempt was to study the
effect of the base plate stiffness on improving the dynamic
characteristics of the pump assembly Scheffer[6], conducted
an experiment to monitor pump condition through vibration analysis This research illustrates the typical steps required to solve resonance problems This paper describes the use of operational deflection shape (ODS) and modal analysis testing for problem-solving
Kumatkar and Panchwadkar[7], carried out a modal anal-ysis of a vertical turbine pump to determine its dynamic char-acteristics such as its natural frequencies and corresponding mode shapes They have analyzed the rotor assembly of VT Pump theoretically, numerically and experimentally The sys-tem is modeled as a lumped mass structure to theoretically determine its torsional natural frequencies and as a continuous system to determine its transverse natural frequencies The numerical model is validated with the results of the theoretical analysis
Nikumbe et al.[8]discussed the modal analysis of vertical turbine pump Natural frequencies of a vertical turbine pump are calculated by performing a modal analysis using the Finite Element Method (FEM) They founded total six modes of vibration for this analysis Experimental analysis is defined
as the study of dynamic characteristics of a mechanical struc-ture Experimental analysis is done by using Fast Fourier Transform (FFT) analyzer During this analysis, exciter anism is done by using an instrumental hammer, as this mech-anism requires a minimum amount of hardware and provides shorter measurement times Comparison between natural fre-quencies with an operational frequency of vertical turbine pump ensured the safe working of the pump
de Souza[9], has used Operating Deflection Shape (ODS) technique to analyze the dynamic behavior of the machine or structure, by determining the existing strains and their proba-ble causes Measurements of phase and of the amplitude of vibration at predetermined points were carried The cause of high levels of vibration of the centrifugal pump was deter-mined and the recommendations for correcting the problem were achieved
Dupac and Rahman [10], have developed and used ODS procedure to monitor relative in-service planar or orbital dis-placements of vertical pump for any signs of excess or incom-patible displacements In such cases, the system is taken out of Figure 1 Measurement locations at the pump unit
Table 1 Overall vibration measurements on the pump unit
Measurement locations Overall velocity before supporting Overall velocity after supporting
Full load test
No load test without coupling
Full load test
No load test without coupling
Trang 3service for full dynamics analysis and subsequent design
mod-ification A combination of ODS, Modal analysis and FEA
has been used to verify any design improvements The
undesir-able structural dynamics is the root cause of poor reliability
Prajapati[11], found out the solution for reducing vibration
in vertical turbine centrifugal pump He enumerated some
methods of identifying vibration in pump and some possible
cause of vibration He found out that the possible cause of
vibration in pump is due to its structure and it is due to either
weight of the motor placed at higher cause maximum vibration
or due to improper misalignment between upper and lower
base part of pump
2 Problem description & task
In this research, dynamic measurements are evaluated for an
axial pumping unit at El-Shabab Pumping Station in the area
of El-Salhiya This pumping station is used to irrigate
9000.5 feddans and consists of 6 pump units; each pump unit
is of discharge 1.5 m3/s, head 11.6 m, 992 rpm, and motor power 1000 kW The vibration problem on Pump unit (1) began after its original motor (a 1000 kW, BROWN BOVERI Type: SOV560wb) was replaced with a new Hungarian motor
as shown inFig 1 The old motor was in service for many years The old motor is 987 RPM and weighs 6200 kg The new motor is 992 RPM and weighs 8600 kg Since the new motor was installed, the vibration on the machine has been extremely rough Therefore, the decision was to modify the motor setup by supporting its base plate with reinforcing con-crete supports at the sides of the base After supporting, the measured vibration level had been duplicated especially on the motor upper and lower bearings and reached a danger value So the task was to determine the source of the high vibrations and the method to overcome this problem in the final motor setup, a part of metal has four webs of 15 mm thickness and each is added by welding to the lower motor
Motor upper bearing
Motor lower bearing
Figure 2 Vibration spectrum measured during full load at motor upper and lower bearings before supporting
Trang 4base to increase the stiffness to overcome the problem of high
vibration due to resonance
3 Results of vibration measurements tests
Overall vibration levels and vibration spectra are measured at
the motor running speed (16.53 Hz) at different locations on
the whole pumping unit parts to determine the dynamic
per-formance for such huge machines installed at the heavy base
plate and located at classI according to ISO 1-10861 This
class defines that up to 2.8 mm/s is a good level, up to
4.5 mm/s is an allowable level, up to 11.2 mm/s is just tolerable level and what exceeds this value is not permissible and dan-gerous Measurements were done during no load condition where the motor was disconnected completely from the pump via the coupling and full load condition Vibration measure-ments were done on 9 locations on the motor upper and lower bearings and pump bearing in the axial, vertical, and horizon-tal directions as shown inFig 1
Vibration measurements were taken before and after sup-porting the motor base at full load and no load conditions
as shown in Table 1 Firstly the measurement results before
Motor upper bearing
Motor lower bearing
Figure 3 Vibration spectrum measured during full load at motor upper and lower bearings after supporting
Trang 5supporting during full load condition indicated that the overall
vibration levels are extremely rough On the motor upper
bear-ing, the overall vibration level reached 6.91 and 9.48 mm/s in
vertical and horizontal directions On the other hand, the
over-all vibration level reached 5.27 and 4.72 mm/s vertical and
hor-izontal directions at the motor lower bearing These levels of
vibration are a danger to the machines and structures where
it transmits to the foundations and structures After that, the
motor was disconnected completely from the pump via the
coupling to check and confirm that the main source of high
vibration level is from the motor The overall vibration levels
are decreased on the motor upper bearing about 24% in the
vertical direction and 50% in the horizontal direction, while they decreased on the motor lower bearing about 84% in the vertical direction and 79% in the horizontal direction Frequency analysis is used to define the exciting frequencies and determine the level of vibration at each specific frequency Also, it is used to determine the sources of vibration, to control vibration levels and solve vibration problems Results of fre-quency analysis shown inFig 2indicated that, there is a high vibration occurs from the mechanical defect at 1 rotational speed Structural modifications were done by adding rein-forced supports to the motor base in order to decrease and control the vibration level
Motor upper bearing
Motor lower bearing
Figure 4 Vibration spectrum measured during no load at motor upper and lower bearings after supporting
Trang 6Results of the overall vibration level after supporting are
extremely increased and reached a danger level according to
ISO 10816 In the case of full load, the overall vibration level
at the motor upper bearing increased about 400% in the
verti-cal direction and 100% in the horizontal direction On the
other hand, the overall vibration level at the motor lower
bear-ing increased about 43% in the vertical direction and 74% in
the horizontal direction Results of frequency analyses in the
case of full load indicated that the vibration amplitude reached
a danger value about 26.3 and 15.7 mm/s in the motor upper
bearing in the vertical and horizontal directions respectively
as shown inFig 3 In the case of no load, the overall vibration
level at the motor upper bearing increased about 180% in the
vertical direction and 65% in the horizontal direction as shown
inFig 4 On the other hand, the overall vibration level at the
motor lower bearing increased about 300% in the vertical
direction and 500% in the horizontal direction Results of
fre-quency analyses in the case of no load indicated that the
vibra-tion amplitude reached a danger value about 11.32 and
6.75 mm/s in the motor upper bearing in the vertical and
hor-izontal directions respectively Vibration level change during
full load and no load conditions before and after supporting
is shown inFig 5
4 Run-up test
A common Way to identify resonances empirically is to oper-ate the equipment across its range of operating speeds while measuring the vibration it exhibits Run-up or coast-down tests, which monitor vibration from standstill to maximum speed and back down, are a quick way to see whether trouble-some resonances are present in the system As shown inFig 6,
a waterfall plot of the spectral data is used to identify a peak vibration level at a certain speed during the run-up a test of the pump unit This plot consists of the 1 vibration ampli-tude being collected simultaneously with a 1 rpm phase read-ing as the machine coasts to a stop runnread-ing speed It could be seen that during the pump starting up, there is a discrete peak
in the magnitude at 1 and it’s a good indication that a reso-nance exists there The speed range includes 10 Hz, 12.5 Hz, 13.75 Hz, 15 Hz, 16.5 Hz, and 17 Hz, 18 Hz and the amplitude
at this speed frequency is 0.0479 mm/s, 0.2077 mm/s, Figure 5 Vibration level during full load and no load conditions
Trang 70.488 mm/s, 0.659 mm/s, 0.17 mm/s, 0.301 mm/s, 0.15 mm/s It
could be seen that the amplitude increases until the rotor
reaches its critical speed (16.5 Hz) and then decreases to the
normal level as the speed continues to change So the speed
at 16.5 Hz which the amplitudes decrease is a possible natural frequency The run-up data identified a natural frequency 1 Figure 6 Run-up test data
Trang 8at 16.5 Hz The resonance is coincident with 1 rotational
speed Vibration from this mechanical defect at 1 rotational
speed is exciting a natural frequency of the pump structure
As a result of operating the pump with its 1 at a resonant
frequency, there was an experience excessive vibration and it
will wear prematurely Corrective actions should be taken to
move the resonant frequency away from the 1 frequency,
through the addition of stiffness (to increase the resonant
fre-quency) or mass (to lower the resonant frefre-quency) to the
struc-ture Another solution is to use a ‘‘tuned absorber” or a ‘‘tuned
mass damper” These devices greatly reduce the amount of
vibration observed at the natural frequency
All the previous results confirmed that characteristics of the
problem are listed below:
The foundation is not rigid enough (weak) to support the new motors
The new motors are heavier than the old one affected the natural frequency of the foundation leading to high vibra-tion levels due to resonance
Vibration from a mechanical defect at 1 rotational speed
is exciting a natural frequency of the pump structure Therefore it is mandatory to perform dynamic structure study to determine the exact stiffness needed The study determines the type and the method of re-enforcing the structure The study includes the
following:- build a numerical model of the structure,
determine its dynamic characteristics,
Design of the re-enforcement to ensure safe and normal operation of the pumps
5 Finite element analysis Finite element analysis (FEA) was used to model the motor structure to estimate the dynamic characteristics using ANSYS WORKBENCH 14.5 The FEA model was built for the orig-inal motor structure and simulation is made to find its natural frequencies and mode shapes The model consists of a motor weighing 8700 kg, a steel base, and a concrete foundation Concrete is assumed to be a homogeneous and isotropic mate-rial and to behave in a linear elastic manner The mechanical properties of the concrete are assumed to be modulus of elas-ticity: 32 GPa, Poisson’s ratio: 0.2, and weight density:
2400 kg/m3 Steel is assumed to be a homogeneous and isotro-pic material behaving in a linear elastic manner The mechan-ical properties are assumed to be modulus of elasticity:
200 GPa, Poisson’s ratio: 0.3, and weight density: 7800 kg/
m3 A simple geometrical structure was designed using SOLID WORKS 2010 to simulate the motor structure as shown in
Fig 7 When a 3D model of solid volumes is generated, solid modeling is generally more convenient compared to direct gen-eration Solid modeling is tedious and too much time consum-ing The boundary conditions assumed that the concrete foundation is fully clamped in the two cases including modified and final motor structure setup
6 Model results
Natural frequencies of a symmetric structure occur in orthog-onal pairs as shown inTable 2 The physical significance is that the motor can actually vibrate (bend) in any direction based on the direction of the applied excitation So it is recommended to increase stiffness results in the high natural frequencies The results of the model indicated that the low stiffness of the motor base contributed to the relatively high oscillatory motion of the motor Add stiffeners as proposed will decrease the amplitude of vibration; however, it will not eliminate the source of vibrations The predicted mode shapes are shown
in Fig 8 The possible cause of this problem is due to that, all these motor applications have a high thrust bearing design consisting of 3 angular contact bearings (2 down and 1 up)
Figure 7 Geometrical dimensions of motor and base plate
structure
Table 2 Predicted natural frequencies
Trang 9Mode 1 Mode 2
Figure 8 Normal mode shapes of motor and base plate structure
Trang 10Lack of precision of fits at upper thrust bearing could create
high unbalance due to eccentricity, besides that insufficient
down thrust causing improper loading of the bearing and
affecting stiffness
7 Modified model
Since the natural frequency at 16.5 Hz is at the upper end of
the motor at 1 operating speed, it is recommended increasing
the machine stiffness Increasing stiffness results in a higher
natural frequency To accomplish the change, a part of metal
has four webs of 15 mm thickness and each is added by
weld-ing to the lower motor base as shown inFig 9 The modified
model produced acceptable results Increasing stiffness by
add-ing the four web model leadadd-ing to alters the natural frequencies
of the motor This modification increases the frequency of the
first pair and second bending modes The change at each
nat-ural frequency based on adding the four webs model is shown
inTable 3 Normal mode shapes of motor and base plate
struc-ture after modifications are shown inFig 10
8 Results of vibration measurements after modifications
After achieving the new modifications to the pump unit, a new
measurement was done to indicate the effect of this
modifica-tion on the performance of the pump unit Overall vibramodifica-tion levels and vibration spectra are shown in Table 4 indicating that the vibration level on the pump unit is extremely reduced The overall vibration level reached 3.6 and 2.631 mm/s on the motor non-drive end in the horizontal and vertical directions The overall level decreases about 89% and 86% on the motor drive end in the horizontal and vertical directions respectively The frequency spectrum showed that the measured vibration amplitude is obviously decreased The maximum vibration amplitude reached 0.227 and 0.294 mm/s on the motor non-drive end in horizontal and vertical directions respectively as shown inFig 11 The results after achieving the new modifica-tions indicated that the overall vibration level is in the permis-sible zone of ISO 10816-1
9 Conclusion Dynamic behavior of the pumping system is affected greatly by the changing in the motor weight The low stiffness of the motor base contributed to the relatively high oscillatory motion of the motor Adding stiffeners as proposed decreased the amplitude of vibration The results confirmed that how the dynamic characteristics of the pump structure are improved after applying modifications The increase in the stiffness of the motor base moves the natural frequencies away from
Figure 9 A four web model added to the lower motor base
Table 3 Normal mode shapes of motor and base plate structure
Modes Description Frequency (Hz) before adding stiffness Frequency (Hz) after adding stiffness