Keywords: abrasion; abrasion resistance; aeration; cavitation; chemical attack; concrete dams; concrete pipes; corrosion; corrosion resistance; deterioration; erosion; grinding material
Trang 1ACI 210.1 R-94
Compendium of Case Histories on Repair of
Erosion-Damaged Concrete in Hydraulic Structures
Reported by ACI Committee 210
(Reapproved 1999)
Stephen B Tatro Chairman
Patrick J Creegan Angel E Herrera
James R Graham Richard A Kaden
This report is a companion document to ACI 210R It contains a series of
case histories on hydraulic structures that have been damaged by erosion
from various physical mechanical and chemical actions Many of these
structures have been successfully repaired There were many examples to
select from; however, the committee has selected recent, typical projects,
with differing repair techniques, to provide a broad range of current
exper-ience These case histories cover only damage to the hydraulic surfaces due
to the action of water, waterborne material or chemical attack of concrete
from fluids conveyed along the hydraulic passages In addition to repairs
of the damaged concrete, remedial work frequently includes design
modi-fications that are intended to eliminate or minimize the action that
pro-duced the damage This report does not cover repair of concrete damaged
by other environmental factors such as freeze-thaw, expansive aggregate, or
corroding reinforcement.
Keywords: abrasion; abrasion resistance; aeration; cavitation; chemical attack;
concrete dams; concrete pipes; corrosion; corrosion resistance; deterioration;
erosion; grinding (material removal); high-strength concrete hydraulic structures;
maintenance; outlet works; penstocks; pipe linings; pipes (tubes); pittings; polymer
concrete; renovating; repairs; sewers; spillways; tolerances (mechanics); wear.
CONTENTS
Chapter l-Introduction, p 210.1R-1
Chapter 2-Cavitation-erosion case histories, p 210.1R-2
Dworshak Dam
Glen Canyon Dam
Lower Monumental Dam
Lucky Peak Dam
Terzaghi Dam
Yellowtail Afterbay Dam
Yellowtail Dam
Keenleyside Dam
ACI Committee Reports, Guides, Standard Practices, and
Commentaries are intended for guidance in designing,
plan-ning, executing, or inspecting construction and in preparing
specifications References to these documents shall not be
made in the Project Documents If items found in these
documents are desired to be part of the Project
Docu-ments, they should be phrased in mandatory language and
incorporated into the Project Documents.
James E McDonald Ernest K Schrader
Chapter 3-Abrasion-erosion case histories, p 21O.lR-13
Espinosa Irrigation Diversion DamKinzua Dam
Los Angeles River ChannelNolin Lake Dam
Pine River Watershed, Structure No 41Pomona Dam
Providence-Millville Diversion StructureRed Rock Dam
Sheldon Gulch Siphon
Chapter 4-Chemical attack-erosion case histories, p 210.1R-25
Barceloneta Trunk SewerDworshak National Fish HatcheryLos Angeles Sanitary Sewer System andHyperion Sewage Treatment FacilityPecos Arroyo Watershed, Site 1
Chapter 5-Project reference List, p 210.1R-32
CHAPTER 1-INTRODUCTION
This compendium of case histories provides tion on damage that has occurred to hydraulic structuresand the various methods of repair that have been used.ACI Committee 210 has prepared this report to help oth-ers experiencing similar problems in existing work.Knowledge gained from these experiences may help
informa-ACI 210.1R-94 became effective Nov 1.1994.
Copyright 8 1994, American Concrete Institute.
All rights reserved including rights of reproduction and use in any form or by any means, including the making of copies by any photo process, or by any elec- tronic or mechanical device, printed, written, or oral, or recording for sound or visual reproduction for use in any knowledge or retrieval system or device, unless permission in writing is obtained from tbe copyright proprietors.
210.1R-1
Trang 2210.1R-2 ACI COMMITTEE REPORT
avoid oversights in design and construction of hydraulic
structures and provide guidance in the treatment of
future problems
Erosion of concrete in hydraulic structures may occur
as a result of abrasive action, cavitation, or chemical
attack Damage may develop rapidly after some unusual
event such as a flood or it may develop gradually during
normal continuous operation or use In most cases where
damage has occurred, simply replacing the eroded
con-crete will ensure immediate serviceability, but may not
ensure long-term performance of the structure
There-fore, repair work usually includes replacing eroded
concrete with a more resistant concrete and additional
surface treatment, modifying the design or operation of
the structure to eliminate the mechanism that produced
the damage, or both A detailed discussion of
mechan-isms causing erosion in hydraulic structures, and
recommendations on maintenance and repair, is
con-tained in ACI 210R
When damage does occur to hydraulic structures,
repair work poses some unique problems and is often
very costly Direct access to the damaged area may not
be possible, or may be limited by time, or other
con-straints In some cases, such as repair to spillway stilling
basin floors, expensive bulkheads and dewatering are
required It may not be possible to completely dry the
area to be repaired or maintain the most desirable
temperature A great deal of planning and scheduling for
repair work are normally required, not only for the
repairs and access, but also for control of water releases
and reservoir levels If time permits, extensive
inves-tigation usually precedes planning and scheduling to
determine the nature and extent of damage Hydraulic
model studies may also be necessary to evaluate possible
modifications in the design or operation of the facility
This compendium provides the history on 21 projects
with hydraulic erosion damage They vary in size and
cover a variety of problems: 8 with cavitation damage, 9
with abrasion-erosion damage, and 4 with erosion
damage from chemical attack Table 1.1 summarizes the
projects Each repair was slightly different Each history
includes background information on the project or
facil-ity, the problem of erosion, the selected solution to the
problem, and the performance of the corrective action
Histories also contain references and owner information
if further details are needed
CHAPTER 2-CAVITATION-EROSION
CASE HISTORIES DWORSHAK DAM
North Fork, Clearwater River, Idaho
BACKGROUND
Dworshak Dam, operational in 1973, is a straight-axis
concrete gravity dam, 717 ft high, 3287 ft long at the
crest, and contains 6,500,000 cubic yards of concrete Inaddition to two gated overflow spillways, three regulatingoutlets, 12 ft wide by 17 ft high, are located in the spill-way monoliths The inlet elevation for each regulatingoutlet is 250 ft below the maximum reservoir elevation.Each outlet jet is capable of a maximum discharge of14,000 fij/s
Outlet surfaces are reinforced structural concreteplaced concurrently with adjacent lean, large aggregateconcrete Coatings to the outlet surfaces were appliedduring the original construction In Outlet 1, the wall andinvert surfaces from the tainter gate to a point 50 ftdownstream are coated with an epoxy mortar having anaverage thickness of % in The same area of Outlet 2 wascoated using an epoxy resin, approximately 05 in inthickness Outlet 3 was untreated
The outlets were operated intermittently at variousgate openings for a period of 4 years between 1971 and
1975, resulting in a cumulative discharge duration ofapproximately 10 months The three outlets were notoperated symmetrically; outlets 1 and 2 were used pri-marily
PROBLEM
Inspection in 1973 showed minor concrete scaling ofthe concrete wall surfaces of Outlets 1 and 2 One yearlater, in 1974, serious erosion had occurred at wallsurfaces of both outlets immediately downstream of thewall coatings, 50 ft from the tainter gate Part of this wallarea had eroded to a depth of 22 in., exposing and evenremoving some No 9 reinforcing bars In the wall sur-faces downstream of Outlet 1 medium damage, up to 1
in depth of erosion, also occurred in over 60 squareyards of surface, bordered by lighter erosion Everyhorizontal lift joint (construction joint) along the path ofthe jet, showed additional cavitation erosion
SOLUTION
Repairs were categorized as three types:
l Areas with heavy damage, with erosion greater than
2 to 3 in., were delineated by a 3-in saw cut andthe interior concrete excavated to a minimumdepth of 15 in (Fig 2.1 and 2.2) Reinforcementwas reestablished and steel fiber-reinforced con-crete (FRC) was used as the replacement material
l Areas with medium damage, where the depth oferosion was less than 1 in., were bush-hammered to
a depth of % to 1 in and dry-packed with mortar.The mortar, if left untreated, would easily havefailed when subjected to the high velocity discharge
l Areas with minor damage, surfaces showing a blast texture, were not separately treated prior topolymer impregnation The entire wall surfaces ofOutlet 1 were then treated by polymer impregna-tion from the downstream edge of the existingepoxy mortar coating to a distance 200 ft down-stream
Trang 3sand-REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1 R-3 TABLE 1.1 - SUMMARY TABLE OF PROJECTS COMPRISING THIS REPORT
Reference page
210.1R-2
Year
Authority redesign Stilling basin Montana Bureau of Cavitation Various overlays
RecIamation 1966
Espinosa Irrigation
Diversion Dam
1984 Diversion dam New Mexico
1965 Stilling basin Pennsylvania
Soil vation Service Corps of Engineers
Conser-Abrasion
Abrasion
Steel plate armor
Silica fume concrete
210.1R-13
210.1R-15 Kinzua Dam
Los Angeles River
Channel
210.1R-17 7 1940s Channel California
1963 Stilling basin Kentucky
Proposed Channel Colorado
Corps of Engineers Corps of Engineers SoiI Conser- vation Service
Abrasion
Abrasion
Abrasion
Siiica fume concrete Hydraulic redesign High-strength concrete
Pine River Watershed,
Stilling basin Kansas
Diversion dam Utah
Stilling basin Iowa
Syphon outlet Wyoming
Pipeline Puerto Rico
Concrete tanks Idaho
Sewerage California structures
Corps of Abrasion various Engineers
Soil Conser- Abrasion Surface hardener vation Service
Corps of Abrasion Underwater Engineers concrete Soil Conser- Abrasion Polymer-modified vation Service mortar
Puerto Rico Chemical attack PVC lining Aqueduct &
Sewer Authority Corps of Chemica l attack Linings Engineers
City of Los Chemical attack Shotcrete and Angeles PVC liners
210.1R-20
210.1R-22 Providence-Millville
Diversion Structure
Red Rock Dam 210.1R-23
Sheldon Gulch Siphon 210.1R-25
Los Angeles Sanitary
Sewer System and
Damage to the epoxy mortar was minimal and located PERFORMANCE
near the outlet gate This area was repaired with new
epoxy
The polymer impregnation process involved drying all
the surfaces to a temperature up to 300 F to drive off
water and then allowing the surface to cool to 230 F
Monomer was then applied to the surface using a vertical
soaking chamber Excessive monomer was drained and
the surface was polymerized by the application of
approx-imately 150 F water
Operation of the outlets from the time of repair in
1975 until 1982 has been minimal averaging 1400 ft3/s
per outlet with peak discharges of 3600 ft3/s per outlet.Durations of usage are not known After 1982 outlet dis-charges increased, with durations exceeding 50 days.Inspections performed in 1976, the year after therepairs, showed no additional concrete damage except forsome minor surface spalling adjacent to a major pre-existing crack in an area of dry-packed mortar The
Trang 4210.1R-4 ACI COMMlTTEE REPORT
Fig 2.1-Dworshak Dam Detail showing depth of erosion behind reinforcing steel
Fig 2.2-Dworshak Dam Extent of outlet surface preparation prior to concrete and mortar placements
spalled area was patched with epoxy paste, except that
the epoxy paste did not bridge the crack this time Epoxy
resin coating repairs applied to Outlet 2 showed some
failures,
Inspections in 1983 and 1988 showed that epoxy
mor-tar coatings in Outlet 1 continued to perform well Small
areas of damage, typically spalls, are periodically repaired
with a paste epoxy Epoxy resin coatings in Outlet 2 are
repaired more frequently but are performing adequately
Surfaces repaired with FRC and mortar and subsequently
polymer-impregnated showed negligible damage
Poly-mer-impregnated parent concrete shows a typical matrix
erosion around the coarse aggregate to a depth of 1
/ 4-in.,and lift joints exhibit pitting up to 3
/ 8-in deep Surfaces
along lift joints not polymer-impregnated show erosion
up to 3 / 4-in in depth and a general surface pitting greaterthan the companion polymer-impregnated surfaces,
DISCUSSION
Because of variation in the operation of these outlets,both in flow rate and duration, exact time-rate erosionconclusions are difficult to make Recent outlet dischargehas fluctuated annually from moderate flows to none Ingeneral, surfaces that received replacement materials andwere subsequently polymer-impregnated have performedwell Original concrete and new polymer impregnatedconcrete is showing evidence of deterioration, but at arate that is less than the unimpregnated surfaces The
Trang 5REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1 R-5
best performance was by the original epoxy mortar
coat-ing The epoxy mortar in Outlet 1 continues to display an
excellent surface condition, with no cavitation-generated
pitting The epoxy resin coating in Outlet 2 displays good
performance
In 1988, outlets were modified by adding aeration
de-flectors, wedges 27 in wide by 1.5 in high, to the sides
and bottom of each outlet These deflectors were
de-signed to increase the aeration of the discharge jet and
further reduce the cavitation erosion of the outlet
sur-faces Subsequent deterioration of the outlet surfaces has
not been observed
The polymer impregnating of the concrete surfaces of
the outlets was a very complex system of operations
Suc-cess requires continual evaluation of application
tions and flexibility to react to changes in those
condi-tions Issues relating to safety, cost, and field engineering
add significant challenges to a polymer impregnation
pro-ject It is doubtful that this process would be attempted
today under similar circumstances It is more likely that
the aeration deflectors would be the first remedy
con-sidered since they provide a positive solution to the
problem without the higher risks of a failure inherent in
the polymer impregnation process
REFERENCES
Schrader, Ernest K., and Kaden, Richard A, “Outlet
Repairs at Dworshak Dam,” The Military Engineer, The
Society of American Military Engineers, Washington,
D.C., May-June 1976, pp 254-259
Murray, Myles A, and Schultheis, Vem F.,
“Polymer-ization of Concrete Fights Cavitation,” Civil Engineering,
V 47, No 4, American Society of Civil Engineers, New
York, April 1977, pp 67-70
U.S Army Engineer District, Walla Walla, “Polymer
Impregnation of Concrete at Dworshak Dam,” Walla
Walla, WA, July 1976, Reissued April 1977
U.S Army Engineer District, Walla Walla, “Periodic
Inspection Reports No 6, 7, and 8, Dworshak Dam and
Reservoir,” Walla Walla District, Jan 1985
CONTACT/OWNER
Walla Walla District, Corps of Engineers
City-County Airport
Walla Walla, WA 99362
GLEN CANYON DAM
Colorado River, Northeast Arizona
BACKGROUND
Glen Canyon Dam, operational in 1964, is a concrete
gravity, arch structure, 710 ft high with a crest length of
1560 ft The dam is flanked on both sides by high-head
tunnel spillways, each including an intake structure with
two 40- by 55-ft radial gates Each tunnel consists of a
41-ft diameter section inclined at 55 percent, a vertical
bend (elbow), and 985 ft of near horizontal length lowed by a deflector bucket Water first flowed throughthe spillways in 1980, 16 years after completion of thedam
fol-PROBLEM
In late May 1983, runoff in the upper reaches of theColorado River was steadily increasing due to snowmeltfrom an extremely heavy snowpack On June 2,1983, theleft tunnel spillway gates were opened to release 10,000
ft3 / s On June 5 the release was increased to 20,000 ft3 / s
On June 6 officials heard loud rumbling noises comingfrom the left spillway Engineers examined the tunneland found several large holes in the invert of the elbow.This damage was initiated by cavitation, triggered by dis-continuities formed by calcite deposits on the tunnelinvert at the upstream end of the elbow In spite of thisdamage, continued high runoff required increasing thedischarge in the left spillway tunnel to 23,000 ft3 / s byJune 23 Flows in the right spillway tunnel were held at
6000 ft3 / s to minimize damage from cavitation Spillwaygates were finally closed July 23, and engineers made athorough inspection of the tunnels
Extensive damage had occurred in and near the lefttunnel elbow (Fig 23) Immediately downstream fromthe elbow, a hole (35 ft deep, 134 ft long, and 50 ft wide)had been eroded in the concrete lining and underlyingsandstone foundation Other smaller holes had beeneroded in the lining in leapfrog fashion upstream fromthe elbow
SOLUTION
Therepair work was accomplished in six phases: 1) moving loose and defective concrete lining and founda-tion rock; 2) backfilling large cavities in sandstone foun-dation with concrete; 3) reconstructing tunnel lining; 4)grinding and patching of small defective areas; 5) remov-ing about 500 cubic yards of debris from lower reaches oftunnel and flip bucket; and 6) constructing an aerationdevice in the lining upstream of the vertical elbow.Sandstone cavities were filled with tremie concrete be-fore the lining was replaced About 2000 cubic yards ofreplacement concrete was used The aeration slot wasmodeled in the Bureau of Reclamation Hydraulic Labor-atory to ensure that its design would provide the per-formance required
re-The aeration slot was constructed on the inclined tion of the tunnel approximately 150 ft upstream fromthe start of the elbow A small 7-in-high ramp was con-structed immediately upstream of the slot The slot was
por-4 by por-4 ft in cross section and extended around the lowerthree-fourths of the tunnel circumference (Fig 2.4) Allrepairs and the slot were completed in the summer of1983
PERFORMANCE
Because of the moderate runoff in the Colorado Riversince completion of the tunnel repairs, it has not been
Trang 6210.1R-6 ACI COMMITTEE REPORT
Fig 2.3-Glen Canyon Dam Erosion of spillway tunnel invert and sandstone foundation
rock downstream of the elbow
necessary to use the large spillway tunnels However,
shortly after completion of the work, another high runoff
period permitted performance of a field verification test
This test lasted 72 hr with a maximum flow during that
time of 50,000 ft3 / S The test was conducted in two
phases with several interruptions in each for examination
of the tunnel Offsets were intentionally left in place to
evaluate whether the aeration slot would indeed preclude
cavitation and attendant concrete damage The tunnel
re-pairs and air slot performed as designed No sign of
cavi-tation damage was evident anywhere in the tunnel
Aera-tion has decreased the flow capacity of the spillway
tunnels by approximately 20 percent of the original flow
capacity
REFERENCES
Burgi, P.H., and Eckley, M.S., “Repairs at Glen
Can-yon Dam,” Concrete International, American Concrete
Institute, MI, V 9, No 3, Mar 1986, pp 24-31
Frizell, K.W., “Glen Canyon Dam Spillway Tests
Model - Prototype Comparison,” Hydraulics and
Hydro-logy in the Small Computer Age, Proceeding of the
Spe-cialty Conference, Lake Buena Vista, Florida, Aug
12-17, 1985, American Society of Civil Engineers, NewYork, 1985, pp 1142-1147
Frizell, K.W., “Spillway Tests at Glen Canyon Dam,”U.S Bureau of Reclamation, Denver, CO, July 1985.Pugh, C.A., “Modeling Aeration Devices for Glen
Canyon Dam,” Water for Resource Development,
Proceed-ings of the Conference, Coeur d’Alene, Idaho, Aug.14-17, 1984, American Society of Cii Engineers, NewYork, 1984, pp 412416
CONTACT
U.S Bureau of ReclamationP.O Box 25007, Denver Federal CenterDenver, CO 80225
LOWER MONUMENTAL DAM
Snake River, Near Kaloutus, Washington
BACKGROUND
Lower Monumental Dam, operational in 1970, consists
of a concrete gravity spillway and dam, earthfii
Trang 7Original tunnel surfac
Aeration slot
.I8 SECTION A-A Fig 2.4-Glen Canyon Dam Diagram of new tunnel spillway air slot
bankments, a navigation lock, and a six-unit powerhouse
The 86-ft wide by 675-ft long navigation lock chamber,
with a rise of 100 ft, is filled and emptied by two galleries
or culverts, landside and riverside of the lock structure
The landside culvert, which supplies five downstream
lat-erals, crosses under the navigation lock to discharge into
the river The riverside culvert supplies and discharges
water to the upstream five laterals Each lateral consists
of 10 portal entrances approximately 1.5 ft wide by 3 ft
high Plow velocities in excess of 120 ft/s occur in several
of the portals entrances A tie-in gallery exists between
the two main culverts, near the downstream gates, that
equalizes the pressure between the two culverts
PROBLEM
Inspections as early as 1975 revealed that the ceiling
concrete of the landslide culvert was spalled at some
monolith joints to depths of 9 in This may have been
ini-tiated by differential movement of adjacent monoliths
when the lock chamber was filled and emptied Damage
to the invert, at several locations, was irregular, with
erosion a maximum of 18 in deep at the monolith joint,
decreasing to 1 in at a point 10 ft upstream of the joint
Reinforcing steel was exposed Other areas of erosion in
the invert and on wall surfaces were observed, measuring
2 ft square and 2 in deep
Later inspections revealed that portal surfaces nearest
the culverts of the most downstream laterals were
show-ing signs of concrete erosion (Fig 2.5) By 1978, the
por-tal walls, ceiling, and invert had eroded as deep as 3 in
over an area of 5 square ft, exposing reinforcing steel.All four corners of the tie-in gallery experienced ob-vious cavitation damage The damage varied from minorpitting to exposure and undercutting of the 11 / 2-in aggre-gate
SOLUTION
In 1978, the navigation lock system was shut down fortwo weeks for repairs The major erosion damage to thelandslide culvert was repaired by mechanically anchoredsteel fiber-reinforced concrete The smaller areas ofdamage received a trowel application of a paste epoxyproduct Ceiling damage was backfilled with dry-mixshotcrete Portal and tie-in gallery surfaces receivedapplication of a paste epoxy, troweled to a feather edgearound the perimeter
PERFORMANCE
The mechanically anchored fiber-reinforced concretehas performed well to date No additional erosion hasbeen observed Shotcrete patches to the ceiling adjacent
to the joints show continued spalling, but to a lesserextent than prior to repairs
The repairs to the portal surfaces and tie-in gallerysurfaces performed poorly After 1 year of service, ap-proximately 40 percent of the epoxy paste had failed; andafter 3 years, nearly 100 percent has failed Concreteerosion in these areas has subsequently increased todepths of 6 to 8 in in the tie-in gallery and up to 5 to 6
in on the two most downstream portal surfaces
Trang 8210.1R-8 ACI COMMITTEE REPORT
DISCUSSION
Recent inspections have shown that the rate of erosion
has decreased The accumulated erosion of concrete from
certain surfaces is significant; however, subsequent
ero-sion is almost negligible Consequently, repair schedules
are not critical
Paste epoxy was applied to the concrete surfaces
tran-sitioning to feather edges along the perimeter of the
patches Cavitation eroded the concrete adjacent to the
feather edges as weIl as eroding the thin epoxy edges
(Fig 2.5) These new voids undermined the new, thicker
epoxy, and at some point caused another failure of the
leading edge As the leading edge void increased in size,
the failure progressed until little epoxy was left in the
repaired area After erosion of the epoxy patch material,
no further concrete erosion has occurred It appears that
the eroded configuration of the surface is hydraulically
stable
Patch-type repair procedures are not sufficient for this
structure because erosion is initiated at the edge of the
new patch Eventual repairs will replace larger areas of
the concrete flow surfaces and will include substantial
anchoring of new materials
U.S Army Engineer District, Walla Walla, “Periodic
Inspection Report No 6, Lower Monumental Lock and
Dam,” Walla Walla, WA, Jan 1977
U.S Army Engineer District, Walla Walla, “Periodic
Inspection Report No 7, Lower Monumental Lock and
Dam,” Walla Walla, WA, Jan 1981
U.S Army Engineer District, Walla Walla, “Periodic
Inspection Report No 8, Lower Monumental Lock and
Dam,” Walla Walla, WA, Jan 1983
CONTACT/OWNER
Walla Walla District, Corps of EngineersCity-County Airport
Walla Walla, WA 99362
LUCKY PEAK DAM
Boise River, Near Boise, Idaho
BACKGROUND
Lucky Peak Dam, operational in 1955, is 340 ft highwith a crest length of 2340 ft The dam is an earth androckfill structure with a silt core, graded filters, and rockshells The ungated spillway is a 6000-ft-long ogee weirdischarging into an unlined channel The outlet worksconsists of a 23-ft-diameter steel conduit that deliverswater to a manifold structure with six outlets Each outlet
is controlled by a 5.25-ft by 10-ft slide gate Individualflip lips were constructed downstream from each slidegate Downstream of the flip lips is the plunge pool, ex-cavated into the basalt rock, with bottom areal dimen-sions of 150 by 150 ft The outlet alignment and designwere determined by hydraulic modeling The sir outletsoperated under a maximum head of 228 ft with a designdischarge of 30,500 ft3 / S and a maximum discharge vel-
ocity ranging between 88 ft/s and 124 ft/s
PROBLEM
The steel manifold gates have a long history of tation erosion problems The original bronze gate sealswere seriously damaged by cavitation after initial use.Flow rates across the manifold gate frames in excess of
cavi-150 ft/s for many days were common The gate seals werereplaced with new seals made of stainless steel andaluminum-bronze The cast-steel gate frames requiredcontinual repair of cavitated areas In 1975 alone, over
2000 pounds of stainless steel welding rod was manuallywelded into the eroded areas and ground smooth Neatcement grout was pumped behind the gate frames to re-establish full bearing of the gate frames with the concretestructure
The concrete invert and side piers, which separateeach of the six flip lips suffered extensive erosion soonafter the start of operations in 1955 (Fig 2.6) 3 / 4-in.-thicksteel plates were anchored to the piers and invert areasjust downstream of the manifold gates These steel wallplates became severely pitted, as did the downstreamconcrete flip lip invert surfaces In 1968, the damagedplates were again repaired by filling the eroded areaswith stainless steel welding, and grouting behind theplates Deteriorated concrete on the flip lips was re-moved and additional steel plates were installed overthose areas This also failed and repairs commencedagain Deep areas of cavitation damage in the invert andpiers were filled with concrete New 1 / 2-in.-thick plateswere installed These were stiffened with steel beams,welded on 5-ft centers in each direction Deep anchor
Trang 9REPAIR OF EROSlON DAMAGED HYDRAULIC STRUCTURES 210.1R-9
bars were welded to the plate material to hold them in
place Again, the voids under the plates were grouted
But during the next two years, these repairs also failed
In 1974, it was recommended that the outlet be
re-studied hydraulically That year, remaining plate material
was removed Cavities were found penetrating the invert
and through the piers and into the adjacent outlet invert
These voids were crudely filled with FRC in a “field
expedient” manner Much of this FRC was placed in
standing water with little quality control, while adjacent
bays were discharging
SOLUTION
The side piers were redesigned and replaced to
pro-vide vents that would introduce air to the underside of
the jet just downstream of the gates This modification
was intended to prevent additional invert erosion
How-ever, major modifications to the gates and gate frames
were necessary if cavitation erosion was to be eliminated
These modifications were not made since future
power-house construction would reduce and nearly eliminate
the need to use the outlet, reserving the structure for
emergency and special operations use only Steel lining
on the piers was strengthened and replaced Stiffened
steel plates, 11 / 4-in thick, were installed on the piers and
invert Mortar backfill was pumped behind the invert
plates and new concrete placed between pier plates
PERFORMANCE
After one year of above average usage on bays 3 and
4, cavitation was again observed The side piers just
downstream of the gates showed areas of 1 to 2 square
ft that had eroded through the steel plate and into the
concrete about 6 in No erosion of the invert plates or
the “field expedient” FRC occurred Use of these bays
has almost stopped since the new powerhouse became
operational
DISCUSSION
The introduction of air beneath the jet appears to
have cushioned the effects of cavitation on the flip lip
invert However, pier walls continue to erode at an
extra-ordinary rate The cause lies with the design of the gates
and gate frame It is evident that satisfactory
perfor-mance of the structure can never be achieved until the
gates and frames are redesigned and reconstructed to
eliminate the conditions that cause cavitation
REFERENCES
U.S Army Engineer District, Walla Walla, “Lucky
Peak Lake, Idaho, Design Memorandum 12, Flip Bucket
Modifications,” Supplement No 1, Outlet Works, Slide
Gate Repair and Modification, Walla Walla, WA, July
1986
U.S Army Engineer District, Walla Walla, “Periodic
Inspection Report No 6, Lucky Peak Lake,” Walla
Walla, WA, Jan 1985
U.S Army Engineer District, Walla Walla, “Periodic
Terzaghi Dam, operational in 1960, is 197 ft high with
a crest length of 1200 ft The earth and rockfill ment consisting of an upstream impervious fill, clay blan-ket, sheet pile cutoff, and multiline grout curtain, isfounded on sands and gravels infilling a deep river chan-nel The dam impounds Bridge River flow to form theCarpenter Lake reservoir, from which water is drawnthrough two tunnels to Bridge River generating stations
embank-1 and 2, located at Shalalth, B.C., on Seton Lake.Terzaghi Dam discharge facilities are composed of asurface spillway consisting of a 345 ft long free overflowsection; and a gated section with two 25 ft wide by 35 fthigh gates Two rectangular low level outlets (LLO), each
Trang 10210.1R-10 ACI COMMITTEE REPORT
Fig 2.7-Terzaghi Dam Downstream detail of constrictor
ring
8 ft wide by 16 ft high are subject to a maximum heat of
169 ft These outlets were constructed in the top half of
the concrete plug in the 32 ft, horseshoe-shaped diversion
tunnel
PROBLEM
The LLOs were operated in 1963 for about 23 days to
draw down Carpenter Lake to permit low-level
embank-ment repairs Severe cavitation erosion of the concrete
wall and ceiling surfaces downstream of bulkhead gate
slots was observed in the north LLO after the water
re-lease
Dam safety investigations in 1985 identified that the
LLOs were required to permit emergency drawdown of
Carpenter Lake for dam inspection and repair, and to
provide additional discharge capacity during large floods
SOLUTION
The repair consisted of three main categories of work
- repair of damage, improvement to reduce cavitation
potential, and refurbishing gates and equipment
Repair of cavitation damage in the north LLO
in-cluded repair of the walls, crown, and gate slots
Improvements to reduce cavitation potential included1) installing 9-in deep rectangular constrictor frames(Fig 2.7) immediately downstream of the operating gates
to increase pressures in the previously cavitated area, 2)backfilling old bulkhead gate slots and streamlining theexisting LLO invert entrances, and 3) installing piezo-meters in the north LLO to provide information on flowcharacteristics of the streamlined LLO during dischargetesting
Refurbishing gates and equipment included 1) placing leaking gate seals on closure gates; 2) sand-blasting and repainting gates, guides, head covers, and airshafts, 3) cleaning gate lifting rods and replacing bonnetpackings; 4) replacing ballast concrete in north LLOgates and installing ballast cover plates on all gates; and5) refurbishing hydraulic lifting mechanisms of gates
re-Repair concrete was designed to fully bond withexisting concrete Surface preparation included; sawcutting around the perimeter of the damage, chipping toexpose rebar, and installation of grouted dowels Latex-modified concrete was used for all repair work, with steelfiber reinforcement for the cavitation-damaged areas
A total of 26 cubic yards of 3000 psi ready-mixed crete was placed by pumping Maximum aggregate sizes
con-of 3 / 8-in and 3
/ 4-in were used for general repair and vert entrance backfill, respectively
in-The constrictor frames were made from 1
/ 2-in and
3 / 4-in steel plate They were installed in the LLOs bymeans of the following: 1) bolting the constrictor frame
to the existing concrete with a double row of l-in.diameter adhesive anchors at 12-in spacing 2) keying theconstrictor infill concrete into the existing concrete; 3)welding the constrictor frame to the existing gate metal-work in the walls and soffit; and 4) embedding the con-strictor sill shear bar into the existing concrete invert(Fig 2.7)
DISCUSSION
Piezometer readings confirmed that the constrictorframes in the LLOs helped maintain pressures above at-mospheric, indicating that cavitation should not be aproblem in the future
REFERENCES
B.C Hydro, “Terzaghi Dam, Low Level Outlet
Re-pairs-Memorandum on Construction,” Report No EP6,
Vancouver, B.C., Dec 1986
B.C Hydro, “Terzaghi Dam, Low Level Outlet Tests,”
Report No H1902, Vancouver, B.C., Mar 1987.
Trang 11REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-11 CONTACT/OWNER
British Columbia Hydro
Hydrotechnical Department, HED
6911 Southpoint Drive
Burnaby, British Columbia, Canada V3N 4X8
YELLOWTAIL AFTERBAY DAM
Bighorn River, Montana
BACKGROUND
Yellowtail Afterbay Dam, operational in 1966, is a
33-ft-high concrete gravity diversion type structure, 300
ft long, located about 1 mile downstream from Yellowtail
Dam In 1967 following a heavy winter/spring snowpack
in the upstream drainage basin, flood flows passed
through both Yellowtail Dam and the Afterbay Dam
PROBLEM
Divers examined the Afterbay Dam sluiceway and
still-ing basin after the flood flows had passed They found
cavitation damage on the dentates (baffle blocks) and
adjacent floor and wall areas in the spillway stilling basin
Although the cavitation damage was moderate, repairs
were necessary to lessen the likelihood that future
cavitation damage would occur
Damage to the dentates and floor in the sluiceway was
caused by abrasion The relatively low sill at the
down-stream end of the sluiceway was permitting downdown-stream
gravel and sand to be drawn into the stilling area, where
a ball mill-type action ground away the concrete surfaces
In the stilling basin downstream of the reverse ogee
section, cavitation severely eroded the sides of the
den-tates and the adjacent floor areas A similar condition
developed in the sluiceway except that it was caused by
abrasion erosion Since the damage from the two causes
occurred essentially side by side, the situation graphically
illustrated the dissimilar types of erosion resulting from
cavitation and abrasion
SOLUTION
Following the flood, low flows at the dam could be
maintained for only one month That situation required
that all repairs be completed quickly and concurrently In
addition to repairing damaged areas, the downstream sill
in the sluiceway was raised about 3 ft to stop river
gravels from being drawn into the sluiceway Repairs
were completed using a combination of bonded concrete,
epoxy-bonded concrete and epoxy-bonded epoxy mortar,
depending upon thickness of the repair Epoxy used in
this repair was a polysulfide-type material After repaired
materials had been placed and cured, they were ground
to provide a smooth, cavitation-resistant surface
PERFORMANCE
The dam has now been in service about 23 years since
the repairs were made With the exception of a minor
number of spalls, the performance of the repairs hasbeen excellent
REFERENCES
Graham, J.R., “Spillway Stilling Basin Repair Using
Bonded Concrete and Epoxy Mortar,” Proceedings,
Irri-gation and Drainage Specialty Conference, Lincoln, NE,Oct 1971, pp 185-204
Graham, J.R., and Rutenbeck, T.E., “Repair of tion Damaged Concrete, a Discussion of Bureau of
Cavita-Reclamation Techniques and Experiences,” Proceedings,
International Conference on Wear of Materials, St.Louis, MO, April 1977, pp 439-445
CONTACT
Bureau of ReclamationP.O Box 25007, Denver Federal CenterDenver, CO 80225
struc-a high-hestruc-ad spillwstruc-ay locstruc-ated in the left struc-abutment At thisspillway, water enters through a radial-gated intake struc-ture, then passes into an inclined section of tunnel vary-ing in diameter from 40.5 ft at the upper end to 32 ft atthe beginning of the vertical elbow Thereafter, flow fol-lows the 32-ft-diameter tunnel through the elbow and
1200 ft of near horizontal tunnel, exiting into a tion stilling basin-flip bucket, then into the river.During the spring of 1967, heavy rains in the water-shed area of the Bighorn River resulted in high inflowsinto Bighorn Lake behind Yellowtail Dam A total of650,000 acre-ft of flood waters was released through thespillway over a period of 30 days Maximum flow was18,000 ft3 / S
20 ft wide and 6 to 8 ft deep After the tunnel was watered, it was found that a small concrete patch placedduring construction had failed therebv causing the dis-
Trang 12de-210.1R-12 ACI COMMlTTEE REPORT
continuity in the flow that triggered the cavitation
SOLUTION
The tunnel liner was repaired using several systems
depending on the size and depth of the damage Areas
where the damage extended through the lining into the
foundation rock were repaired with high quality
replace-ment concrete Major areas of damage where the erosion
did not penetrate through the concrete lining were
repaired with bonded concrete Shallow-damaged
con-crete was repaired with epoxy-bonded concon-crete and
epoxy-bonded epoxy mortar Surfaces were ground where
necessary to bring tolerances into conformance with
specifications requirements Finally, tunnel surfaces
below spring line were painted with an epoxy-phenolic
paint, to help seal the surface and bond any aggregate
particles that may have been loosened
In order to avoid recurring damage, an aeration device
was model tested in the laboratory and then constructed
in the tunnel a few ft upstream of the point of curvature
of the vertical elbow This aeration slot measured 3 ft
wide and 3 ft deep and extended around the lower three
quarters of the tunnel circumference It was designed to
entrain air in the flow for all discharges up to 92,000
ft3
/ S, without the slot filling with water A 27-in-long
ramp was constructed upstream of the slot which raised
the upstream face of the slot 3 in at the tunnel invert
Under most flow conditions the bottom of the jet was
forced away from the tunnel floor surface The jet
re-mained free for a considerable distance downstream, all
the while drawing air into the jet from the aeration slot
Aeration has reduced the discharge capacity by
approxi-mately 20 percent
PERFORMANCE
It has now been 23 years since the tunnel was repaired
and the aeration slot installed, but flows in the river have
never been sufficient to require use of the spillway
How-ever, a controlled prototype test with flows to 16,000 ft3/s
was conducted in 1969 and 1970 As a result of this test,
less than one percent of the concrete repairs failed and
no cavitation damage was observed, even in areas
down-stream from discontinuities To ensure that the tunnel
will always be ready for the next flow, there is a regular
maintenance program to repair ice damage and remove
calcium carbonate buildups
REFERENCES
Borden, R.C., et al., “Documentation of Operation,
Damage, Repair, and Testing of Yellowtail Dam
Spill-way,” Report No REC-ERC-71-23, Bureau of
Reclama-tion, Denver, CO, May 1971
Colgate, D., and Legas, J., “Aeration Mitigates
Cavitation in Spillway Tunnel,” Meeting Preprint 1635,
National Water Resources Engineering Meeting, Jan
24-28, 1972, Atlanta, GA, American Society of Civil
Engineers, New York, NY, 29 pp
CONTACT
U.S Bureau of ReclamationDenver Office, Code D-3700P.O Box 25007, Denver Federal CenterDenver, CO 80225
The sluiceway downstream of the gate slot has an ogeesection designed very conservatively for 65 percent of thedesign head Upstream of the gate sill the profile is afairly broad three-radius compound curve Accordingly,
no negative pressures should occur anywhere on the crestunder free discharge operation
PROBLEM
Cavitation damage has occurred on the sluiceway crestnear the gate slots on all four bays The damage ex-tended from inside the upstream portion of the gate slot
to a point about 4 ft downstream, extending at an angle
of about 30 degrees to the direction of flow (Fig 2.8).All attempts to repair the eroded concrete with epoxymixtures and steel fiber-reinforced concrete (FRC) in
1973, 1975, and 1977 were unsuccessful Continued itation soon pitted the repaired areas which later pro-gressed to development of major voids By 1980 approxi-mately 80 percent of the previous repair had eroded.During a high water inspection in 1986, sluiceway No 2was flow tested for 4 hr at gate openings of 4, 8, 12 and
cav-16 ft and full opening Characteristic noises of cavitationbubble collapse could be heard intermittently at all gatesettings The highest rate of cavitation activity wasobserved to be with gate openings from 4 to 12 ft.The deepest erosion usually occurred just outside thegate slot with depths ranging from about 8 to 14 in.Downstream of the badly eroded area, the concrete atthe invert was observed to be roughened for another 2 ft.The maximum width of the eroded area varied from 18
to 24 in
The cavitation erosion at the foot of the gate slotdamaged not only the concrete invert but also the lowerpart of the steel liner within the gate slot and an area ofthe wall immediately downstream of the liner The 1986study concluded that the severe concrete erosion at andjust downstream of the gate slots was due to 1) cavitationcaused by vortices originating in the upstream corners ofthe gate slots at small, part-gate operation; and 2) lack ofrounding and lack of offset of downstream edge of gateslot
Trang 13REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-13
SOLUTION
Initially, it was recommended that 1) eroded areas
should be filled with concrete and armored with steel
plates, and; 2) field tests should be conducted to identify
cavitation zones Later, the recommendation was changed
to backfill cavitated areas with aggregate, high
strength (6000 psi) concrete The bond between the
back-fill and the original sluiceway concretes was enhanced by
epoxy bonding agent The top surface of the new patch
and the surrounding original concrete were coated with
an acrylic latex selected through an extensive laboratory
screening process.The work was carried out in the
sum-mer of 1990
PERFORMANCE
In order to test the effectiveness of the repairs, during
the following year it was decided to operate the sluice
gates mostly in the worst range A year later, the
re-paired and coated surfaces began to show signs of pitting
The performance of the repair still did not appear
satis-factory It became obvious that besides repairing the
eroded areas other initiatives were needed to alleviate
recurrence of the problem
DISCUSSION
Based on the observations of the effect of gate
open-ing on cavitation, it was decided to limit gate operation
to that outside of the destructive range Gate operating
orders were rewritten to require “passing over” the rough
zones as quickly as possible without any sustained
operation in those zones
REFERENCES
B.C Hydro, Hydroelectric Engineering Division,
“Hugh Keenleyside Dam, Cavitation Damage on
Spill-way,” Report No H1922, Vancouver, B.C., Mar 1987.
B.C Hydro, Hydroelectric Engineering Division,
“Keenleyside Dam, Comprehensive Inspection and
Re-view 1986,” Report No H1894, Vancouver, B.C., May
1987
B.C Hydro, Hydroelectric Engineering Division,
“Hugh Keenleyside Dam, Cavitation Damage on Spillway,
Field Investigation of Cavitation Noise and Proposed
Gate Operating Schedules,” Report No 2305, Vancouver,
B.C., June 1992
CONTACT/OWNER
British Columbia Hydro Structural Department
HED6911 Southpoint Drive
Bumaby, British Columbia, Canada V3N4X8
CHAPTER 3-ABRASION-EROSION
CASE HISTORIES ESPINOSA IRRIGATION DIVERSION DAM
EspBnola, New Mexico, on the Santa Cruz River
Fig 2.8-Keenleyside Dam Cavitation erosion of concrete invert and adjacent damage to steel liner Maximum depth approximately 9 in.
BACKGROUND
The diversion dam is a reinforced concrete structurethat is capable of diverting up to 13 f& in the EspinosaDitch for irrigation purposes A 50-ft-long reinforced rec-tangular concrete channel, sediment trap, and sluice gatestructures were constructed between the headgate andthe ditch heading A sidewall weir notch is provided inthe rectangular ditch lining to allow emergency discharge
of flood flows back to the river A 24-in.-round sluicegate at the right side of the dam was placed at the slabinvert elevation, to sluice sand and cobbles through thedam and to prevent these materials from entering the ir-rigation ditch head gate The dam is tied back into theriverbanks on either side with small earthen dikes thatprotect the
Trang 14diver-ACI COMMITTEE REPORT
Fig 3.1-Espinosa Irrigation Diversion Dam Erosion damage to the floor blocks
Fig 3.2-Espinosa Irrigation Diversion Dam Steel plate protection added to floor blocks and endsill
floor blocks (Fig 3.1) due to impact and abrasion by the
bedload The bedload consists of gravels and boulders
ranging up to 24 in in diameter The concrete in the
apron in the impact area was abraded to a depth of 6 in
Except for very low flows and flows diverted for
irri-gation, the bedload is carried over the weir
SOLUTION
Repairs were made by extensive structural tions These modifications included the following (Fig.3.2): 1) removing and replacing the top layer of rein-forcement in the apron; 2) removing and replacing thetop 6 in of concrete; 3) protecting the apron with a ?&n
Trang 15modifica-REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-15
steel plate; and 4) replacing the 24-in-round sluice gate
with a 36-in square sluice gate
PERFORMANCE
The structure has been operating satisfactorily since
rehabilitation in 1982
DISCUSSION
Five alternatives were evaluated for the placement of
the diversion dam back into service The ones not
selected as the solution are as follows:
1 Install a reinforced concrete lining inside the walls
and apron of the existing structure
2 Protect the apron with a 1 / 2-in steel plate
3 Remove the entire apron of the structure and
re-place it with one that is adequately reinforced Add
the liner inside the structure
4 Remove the entire structure and replace it with a
new one
REFERENCES
U.S Department of Agriculture, “Espinosa Diversion
Dam, Report of Investigation of Structural Failure,” Soil
Conservation Service, Albuquerque, NM, Nov 1980
U.S Department of Agriculture, “Espinosa Diversion
Dam, Design Engineer’s Report," USDA, Soil
Conserva-tion Service, Albuquerque, NM, Sept 1982
CONTACT/OWNER
State Conservation Engineer
U.S Department of Agriculture Soil Conservation
Kinzua Dam became operational in 1965 The stilling
basin consists of a horizontal apron, 160 ft long and 204
ft wide It contains nine 7-ft-high by l0-ft-wide baffles,
located 56 ft upstream from the end sill The
vertical-faced end sill is 10 ft high and 6 ft wide The basin slab
was constructed of concrete with a 28-day compressive
strength of 3000 psi
The outlet works consists of two high-level and six
low-level sluices A maximum conservation flow of about
3600 ft3/s is supplied by the high-level sluices The
low-level sluices with flared exists containing tetrahedral
deflectors are located 26 ft above the stilling basin slab
Bank-full capacity, 25,000 ft3/s, can be discharged through
these sluices at reservoir elevation 1325 The maximum
24,800-ft3/s record discharge was discharged through the
sluices in 1972 The maximum velocity at the sluice exit
was 88 ft/s
PROBLEM
Because of the proximity of a pumped-storage plant on the left abutment and problems from spray,especially during the winter months, the right side sluiceswere used most of the time Use of these sluices causededdy currents that carried debris into the stilling basin.The end sill was below streambed level and contributed
power-to the deposition of debris in the basin
Divers reported erosion damage to the basin floor asearly as 1969 Also, piles of rock, gravel, and other debris
in the basin were reported About 50 cubic yards ofgravel and rock, ranging up to 8 in in diameter, wereremoved from the basin in 1972 Abrasion-erosion dam-age reached a depth of 3.5 ft in some areas before initialrepairs were made in 1973 and 1974
These repairs were made with steel fiber-reinforcedconcrete Approximately 1400 cubic yards of fiber con-crete was required to overlay the basin floor From thetoe of the dam to a point near the baffles, the overlaywas placed to an elevation 1 ft higher than the originalfloor
In April 1975, divers reported several areas of sion-erosion damage in the fiber concrete Maximumdepths ranged from 5 to 17 in Approximately 45 cubicyards of debris were removed from the stilling basin.Additional erosion was reported in May 1975, andanother 60 cubic yards of debris were removed from thebasin At this point, symmetrical operation of the lowersluices was initiated to minimize eddy currents down-stream of the dam After this change, the amount ofdebris removed each year from the basin was drasticallyreduced and the rate of abrasion declined However,nearly 10 years after the repair, the erosion damage hadprogressed to the same degree that existed prior to therepair
Construction of a debris trap immediately downstream
of the stilling basin end sill was also included in therepair contract Hydraulic model studies showed thatsuch a trap would be beneficial in preventing downstreamdebris from entering the stilling basin The trap was 25 ftlong with a 10-ft-high end sill that spanned the entirewidth of the basin
Trang 16210.1R-16 ACI COMMlTTEE REPORT
0B -CONVENTIONAL CONCRETE, SYLVANIA LIMESTONE AGGREGATE, 5710 PSI (39 MPa)
PENN-0C -CONVENTIONAL CONCRETE, LOS GELES AGGREGATE, 7470 PSI (52 MPa).
AN-0D -SILICA-FUME CONCRETE, LOS GELES AGGREGATE, 11,500 PSI (79 MPa)
AN-0E -SILICA-FUME CONCRETE, VANIA LIMESTONE AGGREGATE, 13,850
In August 1984, after periods of discharge through the
upper and lower sluices, abrasion-erosion along some
cracks and joints was reported by divers The maximum
depth of erosion was about % in The divers also
dis-covered two pieces of steel plating that had been
em-bedded in the concrete around the intake of one of the
lower sluices Because of concern about further damage
to the intake, the use of this sluice in discharging flows
was discontinued This nonsymmetrical operation of the
structure resulted in the development of eddy currents
Sluice repairs were completed in late 1984, and metrical operation of the structure was resumed A diverinspection in May 1985 indicated that the condition ofthe stilling basin was essentially unchanged from the pre-ceding inspection A diver inspection approximately 31 / 2
sym-yr after the repair indicated that the maximum depth of
erosion, located along joints and cracks, was about 1 in
REFERENCES
The next inspection, in late August 1984, found
ap-proximately 100 cubic yards of debris in the basin In
September 1984, a total of about 500 cubic yards of
debris was removed from the basin, the debris trap, and
the area immediately downstream of the trap The rock
debris in the basin ranged from sand sized particles to
over 12 in in diameter Despite these adverse conditions,
the silica-fume concrete continued to exhibit excellent
resistance to abrasion Erosion along some joints
ap-peared to be wider but remained approximately 1 / 2-in
Fenwick, W.B., “Kinzua Dam, Allegheny River, sylvania and New York; Hydraulic Model Investigation,”
Penn-Technical Report HL-89-17, U.S Army Engineer
Water-ways Experiment Station, Vicksburg, MS, Aug 1989.Holland, T.C., “Abrasion-Erosion Evaluation of Con-crete Mixtures for Stilling Basin Repairs, Kinzua Dam,
Pennsylvania,” Miscellaneous Paper SL-83-16, U.S Army
Engineer Waterways Experiment Station, Vicksburg, MS,Sept 1983
Holland, T.C., “Abrasion-Erosion Evaluation of crete Mixtures for Stilling Basin Repairs, Kinzua Dam,